GAS PROCESSING – LIQUIDS RECOVERY
200 MMSCF/day Gas Processing Plant
LOCATION: Grande Prairie, Alberta
MARKET: Gas Processing
CONTRACT VALUE: $16 M
THE CHALLENGE
Our Midstream client had an existing 180MMSCF/day gas processing facility and wanted to add another 400 MMSCF/day processing across two new processing trains. The new expansion was required to have its own inlet, flare, utilities and gas processing trains.

FACILITY DESIGN
- 200 MMSCF/day train throughput
- 629 bbl slug capacity
- 4500 bbl / day Condensate Stabilization
- 7500 bbl/day C3+ Recovery
- 1700 bbl/day C5+ Recovery
THE SOLUTION
- Lump Sum Engineering
- Lump Sum DeltaV Configuration and Commissioning
- Lump Sum Supply of (4) PDC Buildings including MV and LV systems and Control Systems
- DeltaV Control Cabinets and 9 RIO Cabinets.
- Project included 14MW of prime generations via Solar Turbines
- 1200 IO Point Systems
- Integrated FAT Testing in Calgary
- On-site Pre-commissioning and Commissioning